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Using the MELCOR code, we simulated and analyzed a severe accident at a Chinese pressurized reactor 1000-MW (CPR1000) power plant caused by station blackout (SBO) with failure of the steam generator (SG) safety relief valve (SRV). The CPR1000 response and results for three different scenarios were analyzed: (i) seal leakage and an auxiliary feed water (AFW) supply; (ii) no seal leakage or AFW supply; and (iii) seal leakage but no AFW supply. The results for the three scenarios are compared with those for a simple SBO accident. According to our calculations, the SG SRV stuck in the open position would greatly accelerate the sequence for a severe accident. For an SBO accident with the SRV stuck open without seal leakage or an AFW supply, the pressure vessel would fail at 9576 s and the containment system would fail at 124,000 s. If AFW is supplied, pressure vessel failure would be delayed nearly 30000 s and containment failure would delay at least 50000 s. When seal leakage exists, pressure vessel failure is delayed about 50 s and containment failure time would delay about 30000 s. The results will be useful in gaining an insight into the detailed processes involved and establishing management guidelines for a CPR1000 severe accident. (C) 2013 Elsevier Ltd. All rights reserved.
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PROGRESS IN NUCLEAR ENERGY
ISSN: 0149-1970
Year: 2014
Volume: 71
Page: 30-38
1 . 1 1 9
JCR@2014
2 . 2 5 6
JCR@2020
ESI Discipline: ENGINEERING;
ESI HC Threshold:144
JCR Journal Grade:2
CAS Journal Grade:3
Cited Count:
WoS CC Cited Count: 24
SCOPUS Cited Count: 46
ESI Highly Cited Papers on the List: 0 Unfold All
WanFang Cited Count:
Chinese Cited Count:
30 Days PV: 5